1997 Ford F-250
Owner: Steve83         (All of this user's registries on SuperMotors)
From: Memphis, TN, U.S.A.        (Other registries in TN)
Year, Make, & Model: 1997 Ford F-250        (Other Ford F-250s)
Avatar:
Clubs: SuperFord.org        (Other vehicles in this club)
Nickname: Big Red
Mileage: 298000
Engine: 7.3L PSTD
Drivetrain: E4OD, manual-shift BW4407, Dana 50IFS 4600# 3.54 open, Sterling 10.25" FF 6084# 3.55 open
Notes: Bought filthy inside & out, rat nests in valley & air filter, no brakes, 2 working GPs, shattered dash, broken seat, old tires, sloppy shifter, bent t/g, wheel bearing roar, front left u-joint gone, passenger window inop., cruise inop., front & rear receivers, GNH, drop-in bedliner, Carr steps, cross-bed tool box, bed caps & rails, VentShades.
Last Updated: 2/4/2025
Hits: 8194
Album
Folder Hits Comments Created Updated
folder Pre-purchase9001,44301/23/201/23/20
folder Big Red28008,78603/19/219/12/24
folder First Fixes690029,32201/25/202/4/25
    folder Radio & Dash14002,58008/21/2011/14/22
    folder Bed & Fuel Tanks13003,80002/3/2110/29/24
    folder Transmission9001,75504/18/216/22/24
    folder U-joints12001,819010/6/216/1/24
folder 3-inch Drums50078801/29/208/1/24
folder Glow Plugs & Gaskets10011601/29/201/29/20
folder Modifications1009402/10/202/6/24
    folder Western UltraMount 7-foot; Plow1008402/10/244/25/24
folder Technical Info15004,54705/24/2012/30/24
Newest Media Files
Exhaust95.jpg
87 hits | 73.33 KB | Posted: 5/11/24

'95 7.3L DIT Exhaust System
IF THE IMAGE IS TOO SMALL, click it.

1 Engine Charge Exhaust Pipe 6N646
2 Three Way Catalytic Converter 5E212
3 Muffler 5230
4 Nut N602481-S2
5 Muffler Frame Bracket 5260
6 Exhaust Outlet Pipe Frame Bracket 5260
7 ...
InteriorCleaning.jpg
160 hits | 57.79 KB | Posted: 4/10/24

The carpet & upholstery were nasty, so they all came out & got hosed down.
IF THE IMAGE IS TOO SMALL, click it.
Shocks97F250HD.jpg
397 hits | 82.68 KB | Posted: 4/6/24

These are easily the best truck shocks, and the black Energy poly bushings make them that much better. I use them on all my trucks.
IF THE IMAGE IS TOO SMALL, click it.

Front Shocks Gabriel G63455
[url...
TGHandle.jpg
143 hits | 77.11 KB | Posted: 4/5/24

Tailgate Handle Improvements
IF THE IMAGE IS TOO SMALL, click it.

The chromed pot-metal handle presses the center mechanism's levers down to pull the operating rods & release the latches. But as the bellcranks rotate, they angle outward, which ca...
Slider97F250hD.jpg
216 hits | 83.59 KB | Posted: 3/23/24

Rear Window Slider
IF THE IMAGE IS TOO SMALL, click it.

I've had this window for over a year, but I just got around to swapping it in. Silicone grease on the body & gasket lips make installation easier, and prevents leaks by allowing the rubber to r...
BoxLink97F250.jpg
299 hits | 78.09 KB | Posted: 3/5/24

BoxLink
IF THE IMAGE IS TOO SMALL, click it.

Since the original tiedowns are just holes below the bedrail in each stake pocket, I decided to add modern BoxLink plates & (genuine Ford HL3J99286D62AA) ti...
BigRed24.jpg
179 hits | 82.23 KB | Posted: 2/27/24

I had been planning to sell the diesel because I'm not a diesel mechanic, and I didn't really want 2 F250s, and the brown one rides smoother. But after the blizzard, we decided it would be worth keeping a heavy 4WD that can mount a plow, so I'm kinda...
Plow24.jpg
142 hits | 85.61 KB | Posted: 2/27/24

I had to cook up my own mounts for the receivers, and repair the lift frame horns that fit into the receivers, and buy receivers & wiring & a new controller &... But the plow works now, so I guess I'll have to keep this truck a few more years.
IF TH...
BattsTrays24.jpg
190 hits | 108.77 KB | Posted: 2/27/24

After suffering with the batteries that were in it when I bought it for a few years, I decided to do it right for '24. So on Jan 2, before the blizzard had melted, I bought 2 new TestedToughMAX BXT-65-800s and installed them in the dealership parking...
Most Viewed Files
Fuses.jpg
2054 hits | 81.98 KB | Posted: 2/10/20

Fuse Map for '97 F-series Diesel
CLICK IMAGE AGAIN to ensure you have the largest version before saving or printing. Printed to standard letter paper, it can be folded in half & laminated.

See also:
[url=https://www.supermotors.net/registry/media/7...
Voltage.jpg
1853 hits | 90.61 KB | Posted: 2/10/20

Original battery terminals
IF THE IMAGE IS TOO SMALL, click it.
The top 2 are the Left battery; all the others show the Right battery. Probes are either on the CLAMPS (for the higher readings, because the engine is idling & the alternator is the volt...
20200905_144748.jpg
1514 hits | 90.74 KB | Posted: 9/6/20

In addition to the intermittent surge at startup, the PID for TR (Transmission Range) occasionally showed Reverse at startup, so I adjusted the MLPS, shifter, & shift indicator.
IF THE IMAGE IS TOO SMALL, click it.

[url=https://www.supermotors.net/r...
USBPwrPt.jpg
1393 hits | 67.76 KB | Posted: 2/2/20

Even though the whole dash shell has to come out, I need USB power now, so I replaced the Power Point with this dual socket & voltmeter (which shows ~0.3V lower than my meter). I'll probably add a switch later.
IF THE IMAGE IS TOO SMALL, click it.
20200330_001404.jpg
1094 hits | 98.55 KB | Posted: 3/29/20

Because the original terminals were abused, I soldered on some new Copper clamps. I avoided the Lead powder being thrown by the cutting wheel, and used a wood block under the anvil when air-chiseling the old ones off the cables (so I wouldn't shorten...
ATF300Kmi.jpg
1065 hits | 89.91 KB | Posted: 12/30/20

E4OD Pan, Gasket, & ATF (photo sequence is DOWN, then across)
IF THE IMAGE IS TOO SMALL, click it.
With engine at idle, transmission in neutral range, approximately 1 quart (minimum) of fluid should flow per minute through the cooler loop.

Consideri...
20200310_160550.jpg
1038 hits | 77.07 KB | Posted: 3/12/20

These shifter bushings made it much easier to get out of Park, and the junkyard boot (which is NOT identical to the original) looks much better, after was...
NotQuite.jpg
973 hits | 45.79 KB | Posted: 2/10/21

After welding the baseplate to the tube, and copying the float arm, re-assembling the tank hanger was quick & easy. But before dropping it in, it has to be checked - I ended up changing the sender board to get it working perfectly, and then screwed t...
20200330_163102.jpg
856 hits | 87.49 KB | Posted: 4/2/20

The negative terminal was easy: after cutting the original Lead clamp away, stripping enough cable to go in the new terminal, and brushing off the corrosion, I dropped the solder pellet in and torched the terminal until the cable dropped in, pushing ...
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